Daryl333
Well-Known Member
- Joined
- Nov 21, 2018
- Threads
- 47
- Messages
- 462
- Reaction score
- 251
- Location
- Vancouver Canada
- First Name
- Daryl
- Vehicle(s)
- 2017 Mustang GT
- Thread starter
- #16
You keep repeating that it's my car 'NOT THE TUNE'.Idle misfires are not normal. If you have a DTC for a misfire there is a issue.
Did you check to see if you cracked any more spark plugs like the last one which we called from the start?
Did you confirm a misfire or just think it sounds like you are hearing one?
So far 2 well known reputable coyote tuners appear to have the same issue so you deff have something going on with the car.
If you were semi local i would deff come out in person and find that issue for you.
We said nothing about not being able to tune the TB angle??? We tune the 132 all the time so not sure why you are sharing miss information??
Also the fuel system fixed the lean condition not the misfire.
Replacing that spark plug that had the cracked insulator fixed your wot misfire
Yes I know that, again I'm not putting this on the tune, stop saying that shit. I already said the fuel system solved the WOT misfire.There were different plugs in when it went lean at WOT.
You said the the Whipple caused the idle fluctuations seems others don't think so.
Of course I know there's something going on with my car. You think I'm spending all this time and money on nothing??
Do you think that I and others don't know what a stumble/misfire at idle is??
This your email saying the large Throttle body is causing it.
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