Toasteii
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Was doing a 1-3 short stretch pull went fine up untill going into 3rd got locked out and pushed me into 1st saw 8k on the tach no clue if more but it didnt hang at 8k for a long time maybe like half a second at MOST. realised my clutch was sent into obliteration just coasted and prayed. Started the motor still warm reved it up to 6k everything sounded fine throttle response still felt there. Strap towed it home 3 hours later with the engine idling no issues what so ever. engine made no new noise no CEL, cant really test it as it wont move at the moment lol. Was time for a clutch anyway and finally time to get a new shifter in there so this dosent happen again. Ill run a compression test on it. Did I get lucky? Or did I go past the point of no return probably bending a valve?
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. I get a loud continuous "Supercharger whine" sound that pitch scales with RPM increase. Im thinking alternator or maybe a belt pully? Im curious why its doing it now when during the tow home it was perfectly fine and made no noise what so ever. Im wondering if maybe the dealer messed it up or if this is just shear concidence of making the poor alternator or pully experience 8k rpm my voltage still looks good on my battery doesnt go below 14.1 volts at idle.