Abb0nz
Well-Known Member
- Joined
- Jul 16, 2015
- Threads
- 9
- Messages
- 85
- Reaction score
- 18
- Location
- Houston, Tx
- First Name
- Paul
- Vehicle(s)
- 2017 GT
- Thread starter
- #1
...and ended with a new long block.
Driving to work 3 weeks ago the car started running rough and I got a CEL. It cleared 30 seconds later. On the way home it did it again but didn't clear. Took it into Ford who diagnosed a misfire on #7. Further testing showed little compression and a borescope inspection revealed a scored bore and minor damage to the piston. As it turns out, so I was told, the gudgeon/wrist pin was faulty causing the piston to contact the head. It was only minor contact and was possibly contacting for some time which eventually caused the failure, there was never any noise from the engine.
Anyway, I ended up with a new engine. Ford say this is the first time they've seen this, has anyone heard of this happening before?
Cheers
Paul
Driving to work 3 weeks ago the car started running rough and I got a CEL. It cleared 30 seconds later. On the way home it did it again but didn't clear. Took it into Ford who diagnosed a misfire on #7. Further testing showed little compression and a borescope inspection revealed a scored bore and minor damage to the piston. As it turns out, so I was told, the gudgeon/wrist pin was faulty causing the piston to contact the head. It was only minor contact and was possibly contacting for some time which eventually caused the failure, there was never any noise from the engine.
Anyway, I ended up with a new engine. Ford say this is the first time they've seen this, has anyone heard of this happening before?
Cheers
Paul
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