SolarFlare
Well-Known Member
Im just gonna say it......601 with a built short block and TVS at 12 psi is SHIT! if you have to rev it to 8k to eek out 615 you have already failed!
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DeadMight want to add a forth option to ur poll. ( multiple pulls with audible knock)
This is correct. LMS is wrong. There was no audible knock. I told them that when I went to Alternative Auto for dyno day that the owner that did the pulls thought there was possibly predetonation and that I should contact LMS. I did contact them on the phone and email. I emailed my salesman a photo of the dyno. They said it was probably the way the dyno was set up at Alternative Auto. For 11-14, not 15 up. I said I was concerned about the possibilty of pre-detonation and that is could hurt the engine.Your own words OP from post #26.
Now, I'm angry. This is an absolute lie. Completely untrue. I never said I heard any pre-detonation. What I said throughtout this thread is the truth. I cannot believe this. WOW, I have tried to maintain a calm attitude. This shop is dishonest. I am smoking hot.The problem occurred from a factory part failing in the engine, nothing tune related, nothing that the customer did himself, just bad luck with bad gas PERIOD. You cant get garbage gas and expect a 11:1 Engine to live with stock parts.
So here goes, customer went to a dyno day. The dyno operator said to the customer its knocking excessively. He made one more pull and still heard knock (WHICH WE VALIDATED THE CUSTOMER STORY IT IS TRUE). We seen the graph the second run has spots in the graph that had 40 HP difference. Why because the Knock sensor was pulling as much as it could out. But if the gas was literally 87 Octane or not 93 this stuff happens.
Now the customer came back to us and we re-dynoed it and low and behold the factory knock sensor was actually adding timing? Why cause this was several days or week later and the customer had been through the bad tank of gas and it was doing what it was supposed to with correct gas. And no there was no drops in the graph or sounds of knocking when it returned. But unfortunately the damage was already done. Read any car that requires premium gas owners manual and you will see it is required to run premium! Anything other than this can RESULT IN SEVERE ENGINE DAMAGE.
I'm sorry you want to blame Livernois for all this nonsense but in this case we have a smoking gun verifying that there was audible knock from another shop. This happens places get bad gas. I dont know what to tell you we have hundreds of these tunes and these kits out there with no issues.
Look we did what we think is the right thing to do gave the customer a smoking deal on the engine because of what happened. Stop with the nonsense.
Also this car has made over 600 RWHP now and will most likely make even more we are setting the thing to run close to 8000 RPM.
And we are going to make sure the customer drives this car before its released to ensure the drive ability is dam near perfect.![]()
Also, incorrect. It came in to LMS with the same tank of gas it dyno'd with.The problem occurred from a factory part failing in the engine, nothing tune related, nothing that the customer did himself, just bad luck with bad gas PERIOD. You cant get garbage gas and expect a 11:1 Engine to live with stock parts.
So here goes, customer went to a dyno day. The dyno operator said to the customer its knocking excessively. He made one more pull and still heard knock (WHICH WE VALIDATED THE CUSTOMER STORY IT IS TRUE). We seen the graph the second run has spots in the graph that had 40 HP difference. Why because the Knock sensor was pulling as much as it could out. But if the gas was literally 87 Octane or not 93 this stuff happens.
Now the customer came back to us and we re-dynoed it and low and behold the factory knock sensor was actually adding timing? Why cause this was several days or week later and the customer had been through the bad tank of gas and it was doing what it was supposed to with correct gas. And no there was no drops in the graph or sounds of knocking when it returned. But unfortunately the damage was already done. Read any car that requires premium gas owners manual and you will see it is required to run premium! Anything other than this can RESULT IN SEVERE ENGINE DAMAGE.
I'm sorry you want to blame Livernois for all this nonsense but in this case we have a smoking gun verifying that there was audible knock from another shop. This happens places get bad gas. I dont know what to tell you we have hundreds of these tunes and these kits out there with no issues.
Look we did what we think is the right thing to do gave the customer a smoking deal on the engine because of what happened. Stop with the nonsense.
Also this car has made over 600 RWHP now and will most likely make even more we are setting the thing to run close to 8000 RPM.
And we are going to make sure the customer drives this car before its released to ensure the drive ability is dam near perfect.![]()
I think someone mentioned this earlier...but why the heck was the gas not tested then?Also, incorrect. It came in to LMS with the same tank of gas it dyno'd with.
That would be great!Get your car back and be done. When your in the UP let me know if you can swing by Iron Mountain area and we can take out my car, same Magnuson, 3.1 pulley, different CAI, Lund tuned with an MT-82 and see how they compare.
Tim
Any word when you will be picking up the car? What kind of warranty does this motor come with? I'm not completely familiar with the Magnuson setups, did you have a specific number you figured the car would make? If it was me, I'd get the car back and if not completely satisfied, have another tuner tune the car and go that route. Is the car still on the stock throttle body?That would be great!