gqneon
Well-Known Member
- Joined
- Jun 25, 2015
- Threads
- 91
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- 867
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- Location
- Westfield, IN
- Vehicle(s)
- 18 GT PP / Manual
Late finding this threar
I'm a little late finding this thread but I was pointed here by Phil. Let me share my ProCharger experience so far.
I too installed a Procharger Stage 2 kit with an upgraded D1SC head unit. I found the belt included with stage 2 to be entirely too short and had 3 conversations with their tech about it, once before trying it, once after shredding the first belt immediately on startup because of excessive tension, and once again after they assured me it was right and shredding my spare I had bought of the same type and size. I then went to O'Reillys and bought belts in .5" increments longer and found 68.5"(1740mm) to be perfect, as opposed to the 66.9" they put in the kit (1700mm) That's what I'm now running with zero issues. ( I ordered Bando 8PK1740 8-rib belts which are on there now for clarification.)
I too blew off an intercooler hose on the passenger side, after finding that hose to be just a tad too short to really reach without straining. I installed a silicone hump hose to the IC, a 3.5" OD aluminum connector with beaded ends, and then mated it to the kit hose on that side after trimming it back to fit correctly. No issues with that now, and it's clearly making boost.
I also had two conversations about the 3.5" inlet hose to the blower being WAY TOO SMALL. I used heat, windex, stretching, picks, screwdrivers, brute force, and threats of harm to all components present. I ended up having to shave the inside of the hose inlet area with a razor knife tiny increments at a time to get it on. If it ever pops off, I have no idea what I'm going to do about it. I'm trying to source a 3.75" coupler which would match the OD of the inlet perfectly, but have been unsuccessful finding a silicone replacement. I may get a 90* rubber 3.75 hose instead, but want the silicone version if possible. ProCharger insists, like the belt, that it's the perfect fit. I hadn't installed the other silicone tube, so I tried both and measured both and found both to have 3.5" ID on both ends, so it was the part they meant to send.
I ALSO have a Lund remote tune. We got through three revisions, but put it on a dyno for 5th gear pulls yesterday. It doesn't help that the dyno shop I've been using doesn't have a boost module for the dyno, so I used a cheap mechanical gauge. It showed 10-11psi at 7200. So the install is absolutely holding manifold pressure.
The first pull put down 562rwhp and 440 rwtq. Watching my boost gauge it looks like it put down a little over 10psi at redline. Everything on the graph looks great with about 19 degrees until about 4400 rpm, then it quickly dials out timing down to 12.5 degrees. That's HUGE! I'm guessing if I can get past the knock sensor / timing issues, then it's going to put down much more. Lund says these cars take 17-18 degrees on 9-10psi all the time without issue. So fuel or sensor issue I guess? Like the OP I'm seeing about 12 degrees where it matters, the only difference is I routed my PCV and IMRC valving per the book with no deviations, so I don't believe I have any potential underlying issues with my IMRC from potential physical damage from his initial configuration he mentioned. I think this info is useful because I'm seeing the same timing WITHOUT the potential IMRC damage.
I installed the kit myself and used ID1000's and a JMS FuelMax, set to default 25/50% activation at 18v. Car is definitely not lean, about 12.0 on the wideband at the dyno although that wideband could be off some according to the dyno guy, since he said my car has 4 wideband sensors on it which would likely give it better accuracy.
It made about 10-11psi on a regular pull, but when the dyno guy started the car for pull 2, it activated the advancetrak warning system and he didn't know how to clear it and didn't want to unstrap it to drive it 25 feet to clear it (which is what it takes and it cleared the instant I got it into first and started rolling the front tires leaving the shop. ) That pull it hit every bit of 12-13psi towards peak, but made less than stock hp because I'm sure the TB or runner valves probably were partially shut because of the advancetrak warning being on.
So I'm in a hold till I hear back from Lund. Maybe he can shed some light?
He told me that the ProFlow valve surging is typical of these ProCharger kits. I have the stock black ProFlow valve installed and it works fine but anytime you're driving near 0 vacuum (read about 5 inches or less vacuum by factory gauge) it surges like it wants to go, then falls back, then forward, then back. He mentioned the red valve doesn't seem to do this, but maybe that's not been everyone's experience here from reading this thread.
He mentioned being able to mask some of the surging in the tune, but only to a degree. He also noted that I'm only holding (in 3rd pulls anyway) about 14-15 degrees timing, and should be about 17-18. I am running Brisk RR14YS plugs (1 range colder, silver electrode, 0.035 gap, no CEL's and no detected misfires). 93 Octane fuel from QuickTrip (QT) all the time, which is supposed to be a guaranteed gas.
I'm thinking about my order of attack being finding a can of Torco to dump in or a tank of 100 octane and putting it on a dyno again. Then maybe swapping out the exhaust back to stock. Then... hell I don't know.
This exact build tuned by the same guy has a video on youtube putting down another 90 hp and 60 lb/ft that was put together by Evolution performance.
I don't get it. I didn't skimp on anything so I wouldn't have any regrets. It's too early to have regrets in this build.
Hope my experience helps or correlates to some of the info in this thread.
I'm a little late finding this thread but I was pointed here by Phil. Let me share my ProCharger experience so far.
I too installed a Procharger Stage 2 kit with an upgraded D1SC head unit. I found the belt included with stage 2 to be entirely too short and had 3 conversations with their tech about it, once before trying it, once after shredding the first belt immediately on startup because of excessive tension, and once again after they assured me it was right and shredding my spare I had bought of the same type and size. I then went to O'Reillys and bought belts in .5" increments longer and found 68.5"(1740mm) to be perfect, as opposed to the 66.9" they put in the kit (1700mm) That's what I'm now running with zero issues. ( I ordered Bando 8PK1740 8-rib belts which are on there now for clarification.)
I too blew off an intercooler hose on the passenger side, after finding that hose to be just a tad too short to really reach without straining. I installed a silicone hump hose to the IC, a 3.5" OD aluminum connector with beaded ends, and then mated it to the kit hose on that side after trimming it back to fit correctly. No issues with that now, and it's clearly making boost.
I also had two conversations about the 3.5" inlet hose to the blower being WAY TOO SMALL. I used heat, windex, stretching, picks, screwdrivers, brute force, and threats of harm to all components present. I ended up having to shave the inside of the hose inlet area with a razor knife tiny increments at a time to get it on. If it ever pops off, I have no idea what I'm going to do about it. I'm trying to source a 3.75" coupler which would match the OD of the inlet perfectly, but have been unsuccessful finding a silicone replacement. I may get a 90* rubber 3.75 hose instead, but want the silicone version if possible. ProCharger insists, like the belt, that it's the perfect fit. I hadn't installed the other silicone tube, so I tried both and measured both and found both to have 3.5" ID on both ends, so it was the part they meant to send.
I ALSO have a Lund remote tune. We got through three revisions, but put it on a dyno for 5th gear pulls yesterday. It doesn't help that the dyno shop I've been using doesn't have a boost module for the dyno, so I used a cheap mechanical gauge. It showed 10-11psi at 7200. So the install is absolutely holding manifold pressure.
The first pull put down 562rwhp and 440 rwtq. Watching my boost gauge it looks like it put down a little over 10psi at redline. Everything on the graph looks great with about 19 degrees until about 4400 rpm, then it quickly dials out timing down to 12.5 degrees. That's HUGE! I'm guessing if I can get past the knock sensor / timing issues, then it's going to put down much more. Lund says these cars take 17-18 degrees on 9-10psi all the time without issue. So fuel or sensor issue I guess? Like the OP I'm seeing about 12 degrees where it matters, the only difference is I routed my PCV and IMRC valving per the book with no deviations, so I don't believe I have any potential underlying issues with my IMRC from potential physical damage from his initial configuration he mentioned. I think this info is useful because I'm seeing the same timing WITHOUT the potential IMRC damage.
I installed the kit myself and used ID1000's and a JMS FuelMax, set to default 25/50% activation at 18v. Car is definitely not lean, about 12.0 on the wideband at the dyno although that wideband could be off some according to the dyno guy, since he said my car has 4 wideband sensors on it which would likely give it better accuracy.
It made about 10-11psi on a regular pull, but when the dyno guy started the car for pull 2, it activated the advancetrak warning system and he didn't know how to clear it and didn't want to unstrap it to drive it 25 feet to clear it (which is what it takes and it cleared the instant I got it into first and started rolling the front tires leaving the shop. ) That pull it hit every bit of 12-13psi towards peak, but made less than stock hp because I'm sure the TB or runner valves probably were partially shut because of the advancetrak warning being on.
I would drive my car to Boostworks RIGHT NOW if I thought you could give me a some dyno time and get me over this timing hump. It could be fuel, it could be a sensor too. I have a 2.5" Ford Racing Street cat-back and it's a little raspy towards middle-high rpm and I can't help but think it's potentially throwing enough vibration to piss off the sensors, but would hate to go back to stock exhaust.We tuned one at 11.5psi, and it made 710whp. We work with Lund. The car drives fine, and make a ton of power.
So I'm in a hold till I hear back from Lund. Maybe he can shed some light?
He told me that the ProFlow valve surging is typical of these ProCharger kits. I have the stock black ProFlow valve installed and it works fine but anytime you're driving near 0 vacuum (read about 5 inches or less vacuum by factory gauge) it surges like it wants to go, then falls back, then forward, then back. He mentioned the red valve doesn't seem to do this, but maybe that's not been everyone's experience here from reading this thread.
He mentioned being able to mask some of the surging in the tune, but only to a degree. He also noted that I'm only holding (in 3rd pulls anyway) about 14-15 degrees timing, and should be about 17-18. I am running Brisk RR14YS plugs (1 range colder, silver electrode, 0.035 gap, no CEL's and no detected misfires). 93 Octane fuel from QuickTrip (QT) all the time, which is supposed to be a guaranteed gas.
I'm thinking about my order of attack being finding a can of Torco to dump in or a tank of 100 octane and putting it on a dyno again. Then maybe swapping out the exhaust back to stock. Then... hell I don't know.
This exact build tuned by the same guy has a video on youtube putting down another 90 hp and 60 lb/ft that was put together by Evolution performance.
I don't get it. I didn't skimp on anything so I wouldn't have any regrets. It's too early to have regrets in this build.
Hope my experience helps or correlates to some of the info in this thread.
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