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2018 Royal Crimson F1A94 Procharged, TH400 Drag Project

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First laps around the neighborhood

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Procharger crank support info

Bolts for ac pulley, they go thru the non-threaded holes of the damper hub:

PXL_20210724_165555773.jpg
PXL_20210724_165600671.jpg


Bolts for the mandrel and blower pulley, they thread into the damper hub:

PXL_20210724_165633437.jpg
PXL_20210724_165641718.jpg


Looks like this:

PXL_20210724_170653618.jpg
PXL_20210724_170706242.jpg
PXL_20210724_171355526.jpg
PXL_20210724_171947663.jpg


I have reversed the bolts and it didn't have any issues either.
 
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Tweaking things here and there as the car is going through the break in process.

215077017_10158923199289681_2768559925466954611_n.jpg
 
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Well the transmission was giving me fits, but got it sorted out (after the third time working on it while it was hot AF.) Put a good run on the car to get it up through the temp. Stopped for an oil change and some beer :beer:

It's so exciting to be out on the road in the car again.

1627163735195.png
 
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Breaking those miles in

PXL_20210725_134641782.MP~2.jpg
 

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No miles tonight, only an oil change and the front license plate was put back on....stupid state requirements.
 

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That’s still progress in the right direction brother! Maybe you can squeeze in some more miles soon. Perhaps a run down I-35 to the Minnesota/Iowa border and back (602 miles round trip) and you’ll be ready for the next oil change and ready for some good oil and a track outing.
 
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Chopped down a 70 mile sprint after dinner.

PXL_20210731_023657073.MP~2.jpg
 
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120 mile trip today. Celebrated half way with a beer. So smooth that the pup got a nap in. He loved the air conditioning 😆

received_1246592349087472~2.jpeg
 
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Mustang is grounded due to a bad rotor hat. This must have been machined wrong from the start but just showed signs of issues. I reached out to the manufacturer to see if they can help me get a new one.

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1627842397052.png


 

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Was it causing a vibration ?
 
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Was it causing a vibration ?
I felt it on the steering wheel. I thought it just needed an alignment since I took the steering rack out during the engine swap. Someone flagged me down on the highway to tell me to pull over. They thought the lugs were loose. When I jacked the car and spun the wheel, it was obvious how out of round it was.
 
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Alright who knows enough about specing out converters, converter slippage, rear gearing, power delivery of a centri supercharger, etc.. to make a recommendation for me.

Car weighs ~3500
TH400 gearing 2.48/1.48/1
Rear gear 3.15
Tire diameter 27.8
1/8 mile slip earlier this year off footbrake, ~3200 rpm:
  • 1.550 60'
  • 6.089 660'
  • 124.34 660' mph
Car would benefit from hanging around in the higher rpm for the procharger.

I think the converter slip may be way out of spec for the car or said differently, the car needs a different rear gear. Maybe 3.73 - 4.10

Anyone educated enough to pull out some facts/logic?
 
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Alright who knows enough about specing out converters, converter slippage, rear gearing, power delivery of a centri supercharger, etc.. to make a recommendation for me.

Car weighs ~3500
TH400 gearing 2.48/1.48/1
Rear gear 3.15
Tire diameter 27.8
1/8 mile slip earlier this year off footbrake, ~3200 rpm:
  • 1.550 60'
  • 6.089 660'
  • 124.34 660' mph
Car would benefit from hanging around in the higher rpm for the procharger.

I think the converter slip may be way out of spec for the car or said differently, the car needs a different rear gear. Maybe 3.73 - 4.10

Anyone educated enough to pull out some facts/logic?
I called ATI and they argued that it's fine. That they specd it properly. Car is dropping 1,600 rpm per gear change which is not keeping the procharger happy.
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